Thanks guys.
Toystory, The pads are a little low but i think they'll be fine for a awhile. I'll get some knew pads soon which im sure will help alot. I do have to keep a feel for any warping. I might drill some vents in it to keep it cooler.
AnderKart, Thats a great tip on the heel chocks. I have just the idea on how to make some.
Okay, so heres the status. I was able to get it all together and start her up. I put in some gas, granted its been in the can since thanksgiving, It started up pretty quick and was able to take it for a 4-5min test drive. WooHoo!

Was that a blast! I was really surprised at the Pep the lil 3.5HP has. Theres no need to up the engine up to the 6.5 clone i have. I might even have to put an adjustable stop on the gas pedal for when the kids ride it.
The steering was Very Responsive, kinda scary responsive at first. I had to stop and bleed the brakes some more. Once i did that, the brakes worked great! Locked up when you wanted. Might put a spring on the brake pedal just to keep a bit more pressure on the foot then just the back pressure on the master cylinder.
So unfortunately, after a few times around the parking lot, the 3.5 briggs started to bog down. I was running it without the filter on because i hadn't made the adapter yet. After it died I pulled the rope a few times and played with the adjusting screw all the way in and all the way out. I couldn't tell if it was making a difference. It would start for a bit and sound fine but when i gave it gas it would just bog down then would take a few turns to start up again. I made the adapter plate and mounted the filter then tried it again. Would run for a bit then bog down again. Took the filter off and pulled the plug. The plug was a bit damp so wiped it then scotch brite and put it back in. It started up again after a few turns, i could feel good vaccum pressure on the air inlet, then i noticed it started blowing smoke back out the air inlet before it would stall.
If its blowing smoke out of the carb inlet, does that mean its getting to much gas?
I pulled out the adjustment screw and scotch brite it, it looked pretty dirty. Also, I gave the carb a thorough cleaning and changed the fuel pump seal before i even started the Kart build.
Hopefully i can get it figured out by tomorrow. Im anxious to get a better and longer test drive. That thing was a blast for about 5 min.