So I have moved the buggy to a location with more real estate. More space to ride around and tune the carb. Unfortunately this means I get to mess around with it less often.
I started by checking the float height. It seemed as though the float level was too high according to what I've seen online. I adjusted it slightly.
I put a fresh plug in and increased the pilot from 30 to 35. I decreased the main jet from 155 to 145.
I drove around for a while trying to get a feel for where the tune needed work. It seems as though with the larger pilot, the off-idle WOT bog improved. It didn't go away, but no longer killed the engine. It would hesitate, but then accelerate.
The 1/2 throttle stumble seemed to come back.
After about 10 minutes of riding with some three or four 15 second stretches of WOT I went back and adjusted the air screw. I think I turned it in to richen the mix to see if I couldn't work on the bog. I slammed on the pedal and it died. Couldn't get it started back up. I waited like an hour and tried again. Still wouldn't start. Compression felt normal. I didn't check for spark, but it seemed like I was getting spark. It almost wanted to run sometimes. I pulled the plug and it was pretty sooty, very black. I put a new plug in and it still wouldn't start. I didn't have any carb cleaner / starting fluid or I would have tried to start it like that. Next time, I guess I start with a carb breakdown and cleaning. I've taken this carb apart at least a dozen times, so it is very likely that it is dirty.
First world problems.