BKS212
New member
So I have what I've identified as a BKS Kart.
When I got it it had a briggs on it with a 30 series TC and a 72 tooth sprocket, and 10 tooth jackshaft. 20X11x8 rear wheels. With mechanical disc brake.
I ve done quite a bit of work to it.
Now has a hemi predator 212 with stage 1 upgrades as well as other free mods. Also put a new driven unit on, New driver flyweight, cover, and slined hub.
The two problems I'm having are #1 the TC is shifting into high range too soon and staying there even when slowing down, letting off gas, going around corners. So it causes the engine to bog down. Its like your driving a car, dump the clutch, wind out 1st gear, then accidentally go into 4th instead of 2nd, just boys right down.
This didn't start until I decided not to leave well enough alone and get a new TC belt, and the yellow torsion spring.
My old belt was 11/16th wide instead of the 3/4 it should be.
I had the green torsion spring in the #2 position (when i got it it was in the #1)
It ran very well topped out at 50mph, and did decent up steep grades, could soon donuts on a dime.
So I put the new belt on, and the yellow spring in the number 3 position thinking it would be even stronger and hold the shift longer.
Wrong.
It actually was slower up grades now, but same too speed.
Changed to the #2 position, a little better but still not as good as the green spring in #2 and old belt.
The new belt was/is getting chewed up too.
So I tried to put the green back in, couldnt, ended up damaging the old driven too much.
So ordered a new driven. It came with the green spring in the #1 position. It ran decent, but still not as good as the old belt and #2 position .
Still not satisfied I went to the #3 position. Now it's even slower and shifting too soon.
I noticed my front driver and spooned hub were wore out and had play.
Orders both new, problem still exists.
Idk what is up with it. Wether its the driver or driven unit. Or if the flyweight is messed up. Or I have the driven preloaded wrong or what. And why it's chewing the belt up. Used a straight edge on them, they're equal, so don't know why Its chewing it up. At a loss. Which I had just left the old belt on and old driven and spring. It looks like the driver clutch isn't closing up fast enough and is opening too soon.
My other problem is, I have a breather filter on the valve cover and it's just spitting oil out. Covering my air filter, which luckily I have a pre filter on. Changed the oil today on it, 10w30 Mobil 1. Still puking it out the breather. You can just tap the throttle and see it bubbling in the breather. Even had some smoke before I changed the oil coming out the breather. The engine turns about 5500 I think based on a go kart speed calculator I found With my 20 inch tall tires, .90 overdrive TC, 72 tooth sprocket, 10 tooth jackshaft, and GPS verified 50mph with the throttle stop all the way out and the zip tie trick in the gov Spring I found on youtube.
Sorry for the long winded post, but wanted to help others rule out things I've already done/tried to remedy the situation.
I also have a YouTube video of the engine and kart running when it ran good if anyone is interested just to see how it did perform.
Engine
https://youtu.be/zKH4C-WC890
Kart being ridden
https://youtu.be/Z9avWSo2WWE
When I got it it had a briggs on it with a 30 series TC and a 72 tooth sprocket, and 10 tooth jackshaft. 20X11x8 rear wheels. With mechanical disc brake.
I ve done quite a bit of work to it.
Now has a hemi predator 212 with stage 1 upgrades as well as other free mods. Also put a new driven unit on, New driver flyweight, cover, and slined hub.
The two problems I'm having are #1 the TC is shifting into high range too soon and staying there even when slowing down, letting off gas, going around corners. So it causes the engine to bog down. Its like your driving a car, dump the clutch, wind out 1st gear, then accidentally go into 4th instead of 2nd, just boys right down.
This didn't start until I decided not to leave well enough alone and get a new TC belt, and the yellow torsion spring.
My old belt was 11/16th wide instead of the 3/4 it should be.
I had the green torsion spring in the #2 position (when i got it it was in the #1)
It ran very well topped out at 50mph, and did decent up steep grades, could soon donuts on a dime.
So I put the new belt on, and the yellow spring in the number 3 position thinking it would be even stronger and hold the shift longer.
Wrong.
It actually was slower up grades now, but same too speed.
Changed to the #2 position, a little better but still not as good as the green spring in #2 and old belt.
The new belt was/is getting chewed up too.
So I tried to put the green back in, couldnt, ended up damaging the old driven too much.
So ordered a new driven. It came with the green spring in the #1 position. It ran decent, but still not as good as the old belt and #2 position .
Still not satisfied I went to the #3 position. Now it's even slower and shifting too soon.
I noticed my front driver and spooned hub were wore out and had play.
Orders both new, problem still exists.
Idk what is up with it. Wether its the driver or driven unit. Or if the flyweight is messed up. Or I have the driven preloaded wrong or what. And why it's chewing the belt up. Used a straight edge on them, they're equal, so don't know why Its chewing it up. At a loss. Which I had just left the old belt on and old driven and spring. It looks like the driver clutch isn't closing up fast enough and is opening too soon.
My other problem is, I have a breather filter on the valve cover and it's just spitting oil out. Covering my air filter, which luckily I have a pre filter on. Changed the oil today on it, 10w30 Mobil 1. Still puking it out the breather. You can just tap the throttle and see it bubbling in the breather. Even had some smoke before I changed the oil coming out the breather. The engine turns about 5500 I think based on a go kart speed calculator I found With my 20 inch tall tires, .90 overdrive TC, 72 tooth sprocket, 10 tooth jackshaft, and GPS verified 50mph with the throttle stop all the way out and the zip tie trick in the gov Spring I found on youtube.
Sorry for the long winded post, but wanted to help others rule out things I've already done/tried to remedy the situation.
I also have a YouTube video of the engine and kart running when it ran good if anyone is interested just to see how it did perform.
Engine
https://youtu.be/zKH4C-WC890
Kart being ridden
https://youtu.be/Z9avWSo2WWE