porting the cylider head
so this is the third head i have ported now. Not perfect, not sure if there will be any improvement, but I did try to not go all out on it. Worked the runner to bowl edges down on both intake and exhaust. Took the hump from the intake and exhaust and blended it to the valve thingee, took the valleys in the intake down just a tiny bit, and blended them more into the bowl. I tried to blend to about the halfway mark on the intake and exhaust valve thingee (gimme a break i got 3 hours sleep last night) time to go into zombie mode at work.
Also, not pictured, but the stainless valves i got were just over a quarter inch longer than the stock valves. This created some real issues with spacing, so i got a valve cover spacer, and a thicker guide-plate for the pushrods. I ended up doing the following:
valves ~7.22 mm longer,
took rocker rollers, spaced up with a thicker pushrod guide plate
spaced up roller rockers even more (ended up being 2-3 washers IIRC that are M.8 washers.
So the rocker studs now have about (you guessed it) 1/4" less available thread than before. So i went out and bought some m.8 x 1.25 pitch x 45mm allen head studs. These are the same ones used on the rockers, but it looks like the rocker studs actually were put on a lathe or ground on the edges of the allen head to decrease the head diameter to make them fit. I will have to grind mine tonight and double check with the calipers. Not sure how im goign to do this, was thinking file/drill, but now im just thinking ill use my bench grinder with an unused grinding wheel and hands.
While i was figuring out this spacing, i was putting the dry erase marker on the valve tips and checking the spread/sweep of the roller tip using an adjustable POS pushrod (the one i got wasnt long enough). Once I got it spaced correctly. i cut a chrome-moly rod and made sure the halfway point of the ball end fit exactly at the first thread of the valve lash adjustment at zero lash (as it says in the instructions).
Also, i dont know if i mentioned this, but clearance was also a struggle. I had to grind a small portion of the edge of the connecting rod down so the pto side of the cam lobe woudl clear it. Also had to flatten out the spot between lobes just about 10-20 thousandths as the rod was hitting it there too. After all that, I am thinking there is hope. There is light at the end of the tunnel, or im just hallucinating from lack of sleep.